Tag Archives: Progress

A 2017 Update

Well as the blog hasn’t been updated in a while, I thought I would take some time and post an update.

Jordan

1966 Series 2:

The car was sold the tail end of 2016 as an unfinished project.  progress stalled on the car and never really got going again.

2006 Disco 3

The car is still going, recently had a handbrake module replaced.  Another repair carried out by land rover was to resolve a recall issue of oil in the brake system.  This had already been done once but the issue re occurred, so they eventually sorted it again.

Disco 2

Since selling the Series 2 Jordan has also purchased a Disco 2 4 ltr V8.  Initially it was sold as the previous owner had put diesel in the tank and tried to start it so some basic work was carried out the car is now taxed and tested and back on the road.

Ian

1983 Ninety

Following a change of job and moving away in May 2016 I don’t have day to day involvement with my car any more, but it is still going driven by my dad on a daily basis.

At the end of October 2016 we made a small addition to the car to allow us to sleep inside it while going to watch Wales Rally GB, this involved some support bars and sheets of marine ply.  Made for a very handy night out kept out of the elements, will post some photos of this later.

Other issues at the moment with the car is the Wipac LED side lights keep blowing fuses up to 15A so more investigation is required.

Nick

1986 110

No change on this yet the car is still as it was when picked up.

Disco 1

Still owned but currently not used.

2001 Disco 2

The car previously owned by Jordan is now mainly used for spare parts.

Disco 2

A TD5 Auto car which has some off road modifications such as tyres bumpers, LED light bar.

Kelsey & Pete

2006 90 TD5

Kelsey and Pete still use this car, recent additions of some 5 bar tread plate, apart from that the car is mostly used on road.

Tom

1993 90 300TDi

Following the rebuild not heard of any more issues with the car, still see it driving around.

Matthew

People are told, if you can’t say anything nice about a person, don’t say anything…

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Toms Car : More Progress

Well today included more progress on Tom’s car, we have now removed the front end bodywork from the car.  We are now in the process of removing all the other body to chassis fixings and the other connections such as wiring and heater controls.

Hopefully we will be able to make more progress over the rest of the weekend and also taking and uploading some more photos.
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Next steps will include lifting the body as well as fitting some new parts to replace some of the more… delicate… parts of the car. Updates to follow!

Tom’s Car : Started

Well last night we finally got round to starting work on changing Tom’s chassis.  This time round we are going to try and take the body off the car in one piece so that we haven’t got to worry about lining all the panels back up at the end of it.

To do this we have got 3 editions of Land Rover Monthly, which handily show the the process using a 2 post ramp to remove the body.  while we are reliant on human power we think it can be done.

So last night we carried out the following steps:

  • Removed the 10 M8 x 20 bolts from the rear of the tub to cross member tabs
  • Removed the 4 screws holding the filler neck to the tub
  • Removed the Gear lever
  • Removed handbrake cable
  • Removed front bumper

The next steps will be undoing the other connections between body and chassis such as fixing bolts electricals and ancillaries then looking to remove the wings and bonnet to make the body work removal easier.

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Start of a journey

Well Tuesday 9th June marked the start in our next journey, the delivery of the chassis for the 300tdi 90.

Over coming months we are going to be doing the chassis swap on this car and hopefully documenting it the blog.

Keep an eye out for progress and photos.  The plan for this one might be to lift the body off in one go so we all need to hit the gym a bit.

Daisy Pains

Well another quick update, recently we have had a couple of little issues with Daisy the TD5 90, it all started with a bit of wet weather, when trying to drive the engine warning light came on and throttle response stopped.

After using diagnostics the fault showed up in the computer as Driver Demand, after a bit of looking we thought it was the EGR valve, a bit of inspection showed that it was a bit clogged so we fitted an egr blanking kit.  that seemed to do the trick for a little while.

Then a couple of weeks later the same issue happend again! unimpressed we decided to go to the next possible cause the accelerator pedal, we had purchased one off ebay at the same time as the EGR valve so put it back in and the fault remained the same.

We noticed that the fault was caused when pressing the clutch, so replacement of the switch on the clutch pedal with MSK100050 [MSK500010] seems to have sorted the issues for now.

November Update

Well after being quiet for a while since we updated the site so here is where we are up to at the moment.  Pictures of the cars will follow soon.

Car 1 –

The last update showed the van sides and roof bolted in place.  Since then we have fixed the inner sills and seat box in place, offered up the floor panels for a fit.

We have also replaced the carb that was originally on the car as when it ran there was a terrible misfire, we now put this down to an assumption the rotor arm moved one direction where it actually went the other so the ignition was only right on 2 cylinders.

With the running sorted we have actually had a short drive around and the engine seems to run very nicely indeed.  Hopefully will add a video to show this soon.

The bonnet has now been rubbed down and ready to paint, with the wings to follow.

Car 2 –

Not much has happened for now with the car still gently running it in driving most days.  We ventured on a 2 hour drive out to Betws-Y-Coed to watch the Cambrian rally in the middle of October, on the way home the car cut out with a diesel leak, eventually we got it home.

On the Sunday after the cause turned out to be the Fuel lift pump, as we revved the engine a mist was seen coming out the bulkhead side.  This was replaced and has run fine since.

We also fitted a pair of Wipac 100w 8″ spot lamps on the front for helping with night time driving on the dark lanes in the area,

That was until today, where got in it this morning and it wouldn’t turn over. Not sure what the issue is at present but will be looking in to it.

Car 4 –

Well progress on this car has moved on a bit now.  Body panels have been repaired painted and refitted, the rear electrics have been fitted.  A set of standard lamps had been fitted but as the owner turned 21 our birthday present to him was a set of wipac LED lamps for front and back.  The issue this has now caused is the need to change from a 2 pin flasher relay to a 4 pin set up.

The hope is to have the car rebuilt and in for MOT by the end of November.

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Car 1 : Wiring started

Last week showed yet more progress on the car, the tub was bolted down to the chassis fully, the sides and roof were bolted down to the tub and the inner sills put in place, so the shape of the car is now fixed.  with it being mostly covered we then moved on to other jobs that were needed.

Over the weekend we started to look at the wiring of the car, the autosparks loom is set up on the car and now just needing to find where the connections go to.

So far we have the start system set up so with a key we can turn the engine over, next up will be making sure the warning lamps for the engine work.  When the engine wiring is all done and we are happy we can then progress to fitting the wings and lights.

Car 1 : Update on rebuild

Well here is a long awaited update on the progress of car 1.

In the last update the tub had been painted and the cappings put on, wiring loom threaded in to chassis, brakes completed, steering.

Since this the seatbox has been painted green, bits on it have been detailed in black such as the latches for the seat tops.  The rear body work sections have also been painted green and bolted on to the black roof.  This is now sat on the tub in place ready to be bolted down when we are ready.

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Plans for this week include getting the inner sills bolted back in place, the seatbox bolted in and the rubbing down and painting of the wings and bonnet.  they will all be fitted once we have the engine wired up and running correctly.

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We have actually started the engine in the last couple of weeks but it just revved so after a bit of diagnosis we think there is an issue with the webber carb that is fitted, it will be replaced in the next 2 weeks with a zenith copy so we shouldn’t have any more issues there.

 

 

Car 4 : Update on rebuild

Well this is a quick update on progress of car 4’s rebuild, there has been so much done to be documented fully.

Front axles rebuilt fully

Chassis rubbed down, repaired & painted

Front & Rear springs replaced with parabolic springs & new shocks fitted

Bulkhead – stripped, repaired, primed, painted, rebuilt & refitted

Front Grill panel – stripped, repaired, primed, painted and refitted

Engine – refurbished, refitted and running.

New exhaust system fitted

Wings & bonnet have been rubbed down primed, painted and fitted

Hopefully we will get a more detailed update with photos soon.

UPDATE:

Over the weekend we did enough work that the engine now fires up using the key and the car has had a short drive around the garden to give it a little test and move around under the car port.

Most of the front electricals have been sorted now.  Side, Dipped, Main and indicator lamps all work, along with the horn.  so left to wire is the washer pump and heater motor.  A rear chassis loom has also been made and will be plugged in tonight and tested for the rear lights.  The next big step is getting the panels all lined up before they get painted and any holes than need drilling can be put in.

Car 2 : Suspension Change

Well after running the car for a few weeks we noticed that the steering wasn’t as good as before the rebuild and we had put it down to castor issues after fitting 2 inch lift springs.

So we purchased a set of AllMakes springs that were standard height and today we got around to fitting them.  We lifted the back of the car letting the axle droop a little then compressed the springs and got them out.  We could slip the new ones back in without the spring compressors so bolted the retaining plates back in and the back was done.

The fronts were slightly harder, we had to remove the bottom nut of the shock absorber compressed the springs and then the shock we had just enough time to pull it out before the shock extended again.  a bit longer and a bit of a harder job but we got it done, in the space of a couple of hours we had all the springs done and it bolted back down again.

This improved the issues we had with steering massively the car now feels pretty much as it did before the rebuild which is great news.

Also while working today we topped up the oil a bit more after the running in and also re bled the brakes.